Click to enlarge

Friday nite practice:
We had some problem with the car misfiring at 5,500rpm, it would smooth out at 6,000rpm.
By turning the boost down from 1bar to .8bar it solved the problem.


Saturday morning practice:
Conrad went out 1st round during practice, it was too early in the morning(7am) he wasn't thinking.
The tires were cold so was the track so he spung out and crack the rear bumper.


Saturday nite practice:
Conrad got the line down and clipping point on the dot, we were pretty sure he'll make the top 8 American D1 drifter.


Sunday morning practice:
Car started to having misfire problem again, but with help from Justin at Rotoray Performance it was fixed.


Sunday 5pm warmup and qualifing rounds:
Conrad did very well during the warmup, but during the qualify rounds the car started to misfire again at 3,000rpm.
It turn out he couldn't drift at all with the misfire so he just ran the course trying.
Sorry to all the fans and supporter of Conrad, we'll get it right next D1(feb).



Conrad/S14
Conrad/S14
Sunisa/Conrad
Conrad/S14

Conrad/S14

Sunisa/Conrad

Team Jspec
D1 S14
D1 S14
Team Jspec

D1 S14

D1 S14

D1 S14
D1 S14
D1 S14
D1 S14

D1 S14

D1 S14

D1 S14
D1 S14
D1 S14
D1 S14

D1 S14

D1 S14